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Split Flow Pumps Save a Shell Project $240,000 Capital and $25,000
per Year Operating Cost
During the development of the Martinez Heavy Gasoline Hydrotreater (HGHT) project, it was discovered that
there were two pump applications for the same process stream. One application
was a large flow and moderate head while the second application was for very low
flows (7 gpm) and a higher head (approx. twice the lower head). The project
Engineering Flow Diagrams were developed with
two sets of pumps. Since the process liquid was over 3OO°F, both sets of pumps
needed to be high temperature API pumps. The rough cost was $40,000 per pump with an
installed cost of over $100,000 each. After the final hydraulics were developed, it
was quickly realized that an API pump operating at 7 gpm was not a very good selection.
So, other alternatives were investigated.
Bechtel’s machinery engineer, Bill Murray, proposed developing a
new pump design where both applications could be handled in the same pump casing.
This would eliminate the need for the two smaller pumps at a project saving of
approximately $240,000. BW/IP agreed to work with Bechtel and Shell to develop a pump (Split Flow) where a
slip stream from the main pump flow would be boosted to the higher head using a
drilled-hole type impeller. This impeller was sized to provide the required head & flow and could
be run dead-headed thus eliminating an expensive minimum flow bypass system for the slip stream.
The pumps were fabricated, tested and started up with the HGHT. They have been
running since start up (June 1996) with no operating or maintenance problems. The
Bechtel engineer applied for and received a US patent for his innovative idea.
The new Split Flow pumps use 60 hp motors. Conventional pumps for this
fractionator reflux service would have used 125 hp motors. Use of the smaller motors
results in an annual kW saving of $25,000 for this installation.
Click to view
the User Case Study
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